L_MC1P - MC_TouchProbe: Inaccurate TP position with I/O input on backplane bus as TP (corrected from V03.18.00)

Corrected from:
Library:  L_MC1P_MotionControlBasic  (FAST Motion)  V03.18.00.252
                      (update via Package Manager)
Response of the new version:
The described inaccuracy of the determined TP position no longer occurs.
 
 
What happens?
Under certain conditions, the touch-probe position determined via MC_Touchprobe is inaccurate. The inaccuracy of the determined TP position corresponds to the distance covered in a PLC cycle. I.e. accuracy decreases with increasing speed.

When does this behaviour occur? 
The behaviour only occurs in the following configuration:
- The actual position comes from a motion drive, e.g. i700 servo inverter and
- the touch probe is evaluated via an EPM-S207 I/O module, terminal on the backplane bus of the controller.
 
Note:
The described behaviour does not occur, when the actual position is evaluated by an external encoder read in via the backplane bus.
 
Which products are affected?
Library:  L_MC1P_MotionControlBasic  (FAST Motion)
 
Short-term measures:
The inaccuracy of the determined TP position corresponds to the distance covered in a PLC cycle.
The difference can be subtracted from the determined TP position.
 
Evaluation/recommendations:
 

URL for linking this AKB article: https://www.lenze.com/en-de/go/akb/201800224/1/
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