L_MC1P: Boot process and page changes of visualisation take long (corrected from V3.13.1)

Corrected from:
Library:   L_MC1P_MotionControlBasic (FAST Motion) from V03.13.01.02 
                 (contained in PLC Designer from V03.13.01)

Response of the new version:
Now the message 'NoValidOverride' will be entered once into the logbook. 
The performance of the system will not be effected significant anymore.
  
What happens?
If certain messages are frequently entered into the controller logbook (WebConfig), the boot process and page changes of the visualisation take much longer.
If the 'NoValidOverride' message occurs, it is e.g. cyclically entered in the transmission cycle into the logbook, i.e. frequently in a row.
As user information, a single logbook entry would already be sufficient if profile generation is not possible due to too small override values and the drive does not move as a result.

When does this behaviour occur?
'0' is assigned to the override inputs (lrOverrideAcc or lrOverrideJerk). 
With these values, profile generation is not possible and the drive therefore does not move.

Which products are affected?
Library:  L_MC1P_MotionControlBasic (FAST Motion)
                (contained in the PLC Designer)

Short-term measures:
Assign values greater than '0' to the inputs 'lrOverrideAcc' and 'lrOverrideJerk'.

Evaluation/recommendations:
The occurrence of the described behaviour can be easily avoided by limiting the minimum override values in the application.
See short-term measure.
 

URL for linking this AKB article: https://www.lenze.com/en-de/go/akb/201500897/1/
Kontaktformular